The valve adjustment brings a few comments: the valves actually needed adjustment, one camshaft was lose (the adjusting gear) and some cam bearings were lose also. This maintenance was needed!
The problem is that once the valve adjustment completed, the mechanic spent about 20 hours to search why the engine didn’t want to work anymore. After a lot of search and 2 weeks, he found that a ground wire in the injection wiring harness was defective. This defect caused the fuel pump to not work anymore.
Once this problem fixed, the mechanic works on the suspension noise. This one is a lot quicker. After a few greasing operations and an inspection of the ball pins supposed (by me) to be the cause of the problem, he discovers that the noise is due to lose suspension arm holders. A few bolts are so lose that they can be turned by hand ! That’s crazy. When I disassembled my other SM’s arms, it was very difficult as these bolts were tight and rusty, but on this car the same bolts are lose.
So it was a big step forward. The engine is working fine, I’m more confident now that valves and camshafts have been inspected and adjusted. The suspension noise finally disappeared, no more cracking noise like a wreck car. Finally, the electrical problem has been a good opportunity to do a maintenance on the electrical circuit and plan to replace the injection wiring harness.
The car is out of the garage early October, but winter is coming and I have to store the car soon, after using it for only 50 kilometers. See you next spring.